Featured Case Study

A 10 MW vertical motor exhibited high vibration levels

Spectrum analysis revealed a combination of soft foot and rotor imbalance as the root causes.

Industry
Heavy machinery
Location
Rajasthan, India
Duration
6 weeks
Completed
July 2024
Motor OverhaulVibration AnalysisHeavy Machine PlantPreventive Maintenance

Key Results Achieved

95%

Reliability Improvement

Achieved 95% uptime after overhaul completion

60%

Maintenance Cost Reduction

Reduced annual maintenance expenses

8%

Energy Efficiency

Improved motor efficiency and power consumption

Project Overview

A 10 MW vertical motor exhibited high vibration levels, measuring 14 mm/s (Horizontal, NDE side) and 8 mm/s (Horizontal, DE side).

The Challenge

A 10 MW vertical motor exhibited high vibration levels, measuring 14 mm/s (Horizontal, NDE side) and 8 mm/s (Horizontal, DE side). Spectrum analysis revealed a combination of soft foot and rotor imbalance as the root causes.

Aging motor fleet with frequent breakdowns
Production losses due to motor failures
High maintenance and operational costs
Need for reliability improvement

Our Solution

Vibrovision team analyzed and corrected Soft foot was corrected, followed by in-situ dynamic balancing, which reduced vibration levels to 1.2 mm/s (NDE) and 0.7 mm/s (DE). The motor was restored to stable operation, ensuring enhanced reliability and reduced risk of failure.

Complete motor teardown and inspection
Rotor and stator refurbishment
Bearing replacement and alignment
Updated protection systems

Implementation Process

1

Detailed motor condition assessment

2

Complete disassembly and component inspection

3

Rotor balancing and stator rewinding

4

Precision bearing installation

5

Updated protection and monitoring systems

Project Outcome

The overhauled motors now operate at 95% reliability with significantly reduced maintenance costs. The plant has achieved consistent production schedules and improved energy efficiency.

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